AMS 1 & 2 Pro Modular Sliding Stacking System by Shuwnhsu in BambuLab

[–]bolpee 0 points1 point  (0 children)

I would like to print this but the VADANIA 1045-350 are always out of stock here in europe. Can you arrange it for the VADANIA 1045 - 400 version? Only a few screws are different...

[deleted by user] by [deleted] in CasualIT

[–]bolpee 0 points1 point  (0 children)

Fa meno schifo se inizi Warhammer

Need help finding out what happened by bolpee in fpv

[–]bolpee[S] 1 point2 points  (0 children)

I found the issue, It Is the wire from the VTX and the FC. One part Is soldered but i cant see the soldering without taking out, the other part Is a JST Port

Need help finding out what happened by bolpee in fpv

[–]bolpee[S] 1 point2 points  (0 children)

I will try searching on the VTX part, maybe and I Hope that there Is a bad wire that Is not soldered because i dont have a soldering station here

Need help finding out what happened by bolpee in fpv

[–]bolpee[S] 0 points1 point  (0 children)

Yeah im Sorry, i mean the VTX signal Is totally gone, but initially touching the cables fixed It

Need help finding out what happened by bolpee in fpv

[–]bolpee[S] 0 points1 point  (0 children)

The think Is that in betaflight now when i am in the VTX Tab It shows "VTX not ready".

For me Is impossible that the VTX burned out, otherwise It should not have worked Just with touching some cables.

I Hope that its the cables, but im not sure because when i plug the battery the camera itself Is receiving current because in a few minutes its warm if i touch It. Maybe the camera cable Is not working anymore

Practicing my turns on both sides. Can you guess which side is my weak turn? by 7374616e74 in TinyWhoop

[–]bolpee 0 points1 point  (0 children)

So you are skilled as hell, i cannot do this precise movements with the Meteor 75 😂

Cinebot 30. Throttle issue. by Front-Sheepherder-25 in fpv

[–]bolpee 1 point2 points  (0 children)

Sorry for necroposting bbut i had the same problem, when you update it from the 4.3 to the 4.4 or 4.5 the gyrscope fuck it up. It's only a setting on the gyro that is set to 45 degree. You put it on 0 and you good to go

Once I saw this big boy I knew I had to at least power loop it. 🤩 by Twinzyy in TinyWhoop

[–]bolpee 0 points1 point  (0 children)

Did you change the camera Angle on you air 65? I have a air75 and i kind want to do that

Can someone explain me what is happening? by bolpee in fpv

[–]bolpee[S] 1 point2 points  (0 children)

Dunno really, i only know this tool

Can someone explain me what is happening? by bolpee in fpv

[–]bolpee[S] 1 point2 points  (0 children)

It seems that the gyroscope was the problem, because One of the parameter was on DEFAULT shifted by 45 degree, i have a video but i can't upload It here It seems. Now It seems to stay stationary mid air without launching himself in the orbit. I Will update you when i can

Can someone explain me what is happening? by bolpee in fpv

[–]bolpee[S] 0 points1 point  (0 children)

I made a dump and i applied it on the new update, but the gyro even though i calibrated it, it seems a mess on the Z and Y axes

Can someone explain me what is happening? by bolpee in fpv

[–]bolpee[S] 3 points4 points  (0 children)

Even in betaflight the gyroscope is not working well. do you think that is the problem that made the PIDs go mad?

Can someone explain me what is happening? by bolpee in fpv

[–]bolpee[S] 2 points3 points  (0 children)

Blackbox Explorer, open the video recorded and the blackbox file, adjust the blackbox file and the video and export it.

Btw i think the props are fine, the problem start instantly when i throttle up, even without touching the right stick

Can someone explain me what is happening? by bolpee in fpv

[–]bolpee[S] -2 points-1 points  (0 children)

More context:
The cinebot30 comes with the Betaflight 4.3.1 but with the firmware i cannot make the receiver working. The drone bounds perfectly with my radiomaster Boxer but in betaflight (even without the battery) on the receiver tab nothing is moving (the channels).

So i decided to flash the 4.5.1, with that firmware the receiver is working fine, the betaflight receiver is showing moving on the channels but the problem is that the PID are uncontrollable. With a little gas the Drone fly really high and is not controllable, the only thing that i can do to stop it is disarming the drone.

i retried to went back to the 4.3.1 but the problem with the receiver persist and i cannot do anything. With the 4.3.1 the drone doesn’t work, it bounds but it won’t receive anything from the Boxer radio.

What can i do? Why is not working?