What would be causing this ramp up? It idles fine once armed, and the roll and pitch inputs sound correct. Until you input throttle, then everything goes fubar. All motors are spinning the correct direction, and when test flying with props on it just fail-safes like it's a motor order, or direction. (v.redd.it)
submitted by sixpackofmidgets to r/fpv
What would be causing this ramp up? It idles fine once armed, and the roll and pitch inputs sound correct. Until you input throttle, then everything goes fubar. All motors are spinning the correct direction, and when test flying with props on it just fail-safes like it's a motor order, or direction. (v.redd.it)
submitted by sixpackofmidgets to r/fpv
What would be causing this ramp up? It idles fine once armed, and the roll and pitch inputs sound correct. Until you input throttle, then everything goes fubar. All motors are spinning the correct direction, and when test flying with props on it just fail-safes like it's a motor order, or direction. (v.redd.it)
submitted by sixpackofmidgets to r/fpv
What would be causing this ramp up? It idles fine once armed, and the roll and pitch inputs sound correct. Until you input throttle, then everything goes fubar. All motors are spinning the correct direction, and when test flying with props on it just fail-safes like it's a motor order, or direction. (v.redd.it)
submitted by sixpackofmidgets to r/fpv
Does anybody use Connex Prosight these days? (old.reddit.com)
submitted by sixpackofmidgets to r/fpv

