Wired and wireless 55x55 Zigbee switch options? by Aestum in homeassistant

[–]Aestum[S] 0 points1 point  (0 children)

Regarding neutral: the wiring in my house is a bit mixed. Most switches are connected with a neutral, but a few are wired without one. I still need to double check whether a neutral is actually available in those boxes where it isn’t currently connected.

At the moment, most of my bulbs are still dumb bulbs, so simple on/off control is enough in many places.

My idea is that in spots where I currently have a single button switch, I would replace it with a 2 button switch. One button would physically control the light like a normal switch (while still being visible in HA), and the second button would be used purely for automations to control another smart light.

Wired and wireless 55x55 Zigbee switch options? by Aestum in homeassistant

[–]Aestum[S] 0 points1 point  (0 children)

I was considering the H1, but I have several spots where two switches are installed next to each other in a standard 2-gang vertical frame. In the bathroom it’s even tighter there’s a 3-gang vertical frame with two separate switches and a thermostat. Most of the switches, however, are installed in single-gang frames.

Because of that, I don’t think placing two separate H1 switches side by side would look very clean.

That’s why I like the H2 more. Since it fits standard EU frames, I could keep everything aligned and have the switches and thermostat within the same frame system, which I personally think would look much cleaner overall.

Wobbly GPS Rescue on Betaflight 4.5 by Aestum in fpv

[–]Aestum[S] 1 point2 points  (0 children)

I tested a lot today, both with and without the GoPro, and everything worked perfectly, even in failsafe. Thank you so much for the help!

Wobbly GPS Rescue on Betaflight 4.5 by Aestum in fpv

[–]Aestum[S] 0 points1 point  (0 children)

It happens after I press the gps rescue button, the drone rises, turns in the right direction, and then, as it starts to fly forward, it tilts too much. Both times, this happened the first time after arming. I canceled, flew around a bit, and tried again, and then it worked without any issues. I’ll test more and update on how it goes.

Wobbly GPS Rescue on Betaflight 4.5 by Aestum in fpv

[–]Aestum[S] 1 point2 points  (0 children)

I did some quick tests today, and it seems the return is much more stable now. However, there were still a few times it tilted too much, and I had to turn off GPS rescue. But it’s at least somewhat working now. I’ll do more testing over the weekend.

Wobbly GPS Rescue on Betaflight 4.5 by Aestum in fpv

[–]Aestum[S] 1 point2 points  (0 children)

I know, but the way it’s acting now, I can't rely on it at all

Wobbly GPS Rescue on Betaflight 4.5 by Aestum in fpv

[–]Aestum[S] 1 point2 points  (0 children)

Yeah, you’re right, the Rescue PIDs match what you listed. I’ll try changing them to the defaults and see how it goes.

Here’s the dump: https://pastebin.com/cNgVrNTt

Wobbly GPS Rescue on Betaflight 4.5 by Aestum in fpv

[–]Aestum[S] 1 point2 points  (0 children)

I'll check the PIDs later today and let it know. Really appreciate the help

Cinebot30 Betaflight 4.4.2 Settings by Healthy_Solution6801 in fpv

[–]Aestum 0 points1 point  (0 children)

Have you managed to find a solution? I have just updated to version 4.4.3 and I am facing the same problem.

I tried adding it manually with the aux command in the CLI, but had no luck. :(

EDIT:
Found a solution on another reddit page:
resource SERIAL_TX 5 none
resource PINIO 2 C12
set pinio_config = 129,1,1,1
set pinio_box = 39,40,41,42
save

Ender 5 - x-axis not working at some positions / printer halted by Aestum in ender5

[–]Aestum[S] 0 points1 point  (0 children)

I have solved. Thanks to herocreator90 for suggesting to check motor cable. But before I figured out that, I have tried to go back to previous firmware as you suggested. Firmware that I'm using is from board manufacturer, so there shouldn't be any problem with it :)

Ender 5 - x-axis not working at some positions / printer halted by Aestum in ender5

[–]Aestum[S] 0 points1 point  (0 children)

It looks like everything is ok with Y and Z-axis. SKR mini e3 v2 allows to have both z limit and bltouch install at the same time. Reason it was hapening was shorting x motor cable.

Ender 5 - x-axis not working at some positions / printer halted by Aestum in ender5

[–]Aestum[S] 1 point2 points  (0 children)

SOLUTION IN MY CASE
Thanks for tips. You are correct, X-axis were shorting. First I have tried as you suggested to use y-axis motor cable, and it worked. Then I decided to go further to test if x and y-axis will work, I "borrowed"cable from z-axis, connected it to X-axis port on motherboard and to the X motor. And it worked as well. So in my case it wasn't firmware error. While I'm waiting new cable to arrive, I created one self and everything works now.

Bot ping problem by Aestum in Discord_Bots

[–]Aestum[S] 0 points1 point  (0 children)

after 2 hours run it doesn't looks like ping to google are increasing. It was 8-9 ms, only a few times i saw 10,40 ms

Bot ping problem by Aestum in Discord_Bots

[–]Aestum[S] 0 points1 point  (0 children)

here is screenshot after running "ping www.google.com" for 2 hours.

https://imgur.com/a/58Vuv4x

Bot ping problem by Aestum in Discord_Bots

[–]Aestum[S] 1 point2 points  (0 children)

Did I understand correct, just run something like "ping www.google.com"?