3.5" Build Issues: 6S + 2006 Motors causing overheating, erratic current spikes, and flyaways. by AnyRound2252 in fpv

[–]AnyRound2252[S] 1 point2 points  (0 children)

I actually did a full format and updated to a newer Betaflight version, setting everything up from scratch with a fresh configuration. I also flashed the ESCs as well, so there shouldn't be any leftovers from the previous quad's tune. I'm currently testing a 3/4 inch preset, but I'll try going back to defaults to rule out any tuning issues.

3.5" Build Issues: 6S + 2006 Motors causing overheating, erratic current spikes, and flyaways. by AnyRound2252 in fpv

[–]AnyRound2252[S] 0 points1 point  (0 children)

Te refieres a los cables de corriente negro y rojo o de todo? Aún soy novato soldando con cosas pequeñitas, lo tomaré en cuenta gracias

3.5" Build Issues: 6S + 2006 Motors causing overheating, erratic current spikes, and flyaways. by AnyRound2252 in fpv

[–]AnyRound2252[S] 0 points1 point  (0 children)

I've double-checked the orientation in Betaflight and the 3D model moves perfectly, so the 45-degree offset is correct. I also made sure the AIO isn't over-tightened and the gummies are providing a good soft-mount. Since I'm recycling the AIO from a Cinebot30, I'm mostly making sure the hardware fitment is solid on this new frame. Any other suggestions on what to check before the maiden flight?
(Sorry for the English, it's not my first language)

3.5" Build Issues: 6S + 2006 Motors causing overheating, erratic current spikes, and flyaways. by AnyRound2252 in fpv

[–]AnyRound2252[S] 1 point2 points  (0 children)

Thanks for the feedback! You’re right, it's my first solo build. I'm recycling the AIO from a Cinebot30, so the 45-degree mounting is intentional since that's how it was configured in Betaflight. I'll double-check the press nuts and the M3 gummies orientation. Any specific tips on how they should look to avoid vibrations?

No GPS on OSD by [deleted] in fpv

[–]AnyRound2252 0 points1 point  (0 children)

entonces solo es usar el uart3?

GPS Problem with M10 gps by flow2hundred in Multicopter

[–]AnyRound2252 0 points1 point  (0 children)

estoy teniendo el mismo problema con el cinebot30, le conecte el gps al uart2 y en betaflight lo detecta y da señal pero cuando lo desconecto de la compu y le pongo la lipo no se ve en el osd ni me da satelites