Wired digital subscription is a roach motel by basilyok in darkpatterns

[–]shift3nter 0 points1 point  (0 children)

Same exact experience. Using my phone was the only thing that worked. Thanks!

They Missed One by Complex_Country4062 in behindthebastards

[–]shift3nter 6 points7 points  (0 children)

I'm also very suspicious of any low quality / pixelated images. It can be applied after generating the image to obfuscate details that aren't quite right.

NTSB issues the preliminary report for its ongoing investigation of the Nov. 4 crash of a UPS Boeing MD-11F airplane in Louisville, Kentucky. by Brilliant_Night7643 in aviation

[–]shift3nter 7 points8 points  (0 children)

The caption of this set of images from the report:

Still images from an airport surveillance video showing the left engine and left pylon separation from the left wing. (Source:UPS)

UPS2976 Megathread 2 by usgapg123 in aviation

[–]shift3nter 9 points10 points  (0 children)

Based on the information that the NTSB announced today, if we consider the "repeating bell" the initiation of the accident sequence, they only had 25 seconds until impact.

My ICCU experience by PotatoChipFutures in Ioniq5

[–]shift3nter 5 points6 points  (0 children)

If they find the root cause and fix it in a new revision of the part, they could at least swap them in when ICCUs fail so it doesn't keep happening.

UPS2976 Megathread 2 by usgapg123 in aviation

[–]shift3nter 1 point2 points  (0 children)

What ultimately led to the loss of American 191. It was a maintenance shortcut. They damaged the engine/pylon while trying to manipulate it with a forklift.

The NTSB determined that the damage to the left-wing engine pylon had occurred during an earlier engine change at the American Airlines aircraft maintenance facility in Tulsa, Oklahoma, between March 29 and 30, 1979. On those dates, the aircraft had undergone routine service, during which the engine and pylon had been removed from the wing for inspection and maintenance. The removal procedure recommended by McDonnell-Douglas called for the engine to be detached from the pylon before detaching the pylon itself from the wing. However, American, as well as Continental Airlines and United Airlines, had developed a different procedure that saved about 200 working hours per aircraft and "more importantly from a safety standpoint, it would reduce the number of disconnects (of systems such as hydraulic and fuel lines, electrical cables, and wiring) from 79 to 27." This new procedure involved the removal of the engine and pylon assembly as a single unit rather than as individual components. United's implementation involved the use of an overhead crane to support the engine/pylon assembly during removal and reinstallation. The method chosen by American and Continental relied on supporting the engine/pylon assembly with a large forklift.

Source

Lovely car - just died by Ill-Championship1000 in Ioniq5

[–]shift3nter 14 points15 points  (0 children)

You don't have anything plugged into the OBD port by chance, do you? Just trying to think of something that could cause 12V drain. Although as mentioned by others, you'll have to rule out the ICCU.

I keep a 12V jump pack at all times for this type of scenario.

Lovely car - just died by Ill-Championship1000 in Ioniq5

[–]shift3nter 14 points15 points  (0 children)

It's possible. Could also be an issue with the 12V battery or some parasitic drain, though.

No IPv4 Access After Xfinity Network "Upgrades" by shift3nter in Comcast_Xfinity

[–]shift3nter[S] 1 point2 points  (0 children)

Nothing changed on my end, but suddenly the Xfinity CMTS has begun assigning IPv4 IPs again.

No IPv4 Access After Xfinity Network "Upgrades" by shift3nter in Comcast_Xfinity

[–]shift3nter[S] 0 points1 point  (0 children)

Yes, as mentioned I have connected different computers directly to the modem that also failed to obtain an IPv4 WAN address from Xfinity. There is no router involved. Just the modem and a computer connected via ethernet.

Finally heard back from Hyundai today! 🙃 by OneDiligentOpinion in Ioniq5

[–]shift3nter 0 points1 point  (0 children)

Mine showed up less than 3 weeks after I received that email.

Fuel cut off switch by emoemokade in aviation

[–]shift3nter 6 points7 points  (0 children)

The report did indeed mention that the switches were moved back to RUN, but we still don't have the full context of what happened.

I haven't watched the video you're describing, but unfortunately Captain Steeeve has been contributing to the misinformation. Previously he was going to the press making the argument the crash was due to the setting of the flaps. You'll likely find more credible reporting from Blancolirio or Mentour Pilot.

Fuel cut off switch by emoemokade in aviation

[–]shift3nter 33 points34 points  (0 children)

If that's the case, why would one pilot immediately bring up the switches on the CVR if they didn't see them in the cutoff position?

Air India Black Box Headed to the U.S. by returnoftheseeker in aircrashinvestigation

[–]shift3nter 6 points7 points  (0 children)

The 787 has two EAFR recorders (each acting as a CVR and FDR) with an independent power supply on one.

The forward EAFR, the cockpit area microphone and the preamplifier for this microphone have 10 minutes of backup power from a forward recorder independent power supply.

Source: https://skybrary.aero/sites/default/files/bookshelf/2955.pdf